Just wanted to show the results of my work over the last 2.5yrs. It started with a bottom job, and I got a little carried away. Ended up completing the following:
1) Repaired cracks and gouges, epoxy filled holes for mounting hardware, and painted hull and deck & binnacle with Interlux Perfection
2) Rebedded all deck hardware, replacing cleats and organizers
3) Built GPS housing and Engine control panel
4) Refinished hatches
5) Replaced chainplates (discussed in earlier thread)
6) Replaced Rudder with FOSS rudder - the improvement in handling is remarkable - better upwind perfomance, and and much better balanced helm. Also replaced quadrant with bronze as old aluminum one was siezed to shaft and significantly corroded. New chain as well.
7) New shaft, PSS shaft seal, and engine mounts
8) Replaced all thu-hulls - and relocated some. Enlarged scuppers to 2-inch, and moved them above the water line. There are four holes now below the water line (there were 8!) - raw water in, head discharge, sink discharge, and speedwheel.
9) Lightning grounding system.
10) Replaced all electrical wiring with marine grade tinned, and heat shrunk all terminals.
11) Replaced all engine hoses.
I sailed the boat hard the last weekend for sea trials in 20 knots (family was NOT onboard - took them out in 10 knots after initial trials). The biggest concern I had was the chainplate area, which I reglassed after cutting away a four foot by 2 inch section in order to remove old and corroded chainplates, and all of this held up beautifully during an intentional jibe (not a full force jibe, but wanted to test the rig with a sudden shock), and a minor knockdown.
The only things that went wrong were:
1) I lost steering b/c I had not tightened the u-bolts on the cable sufficiently (it took sailing closed hauled in 20knots after several trials with full 135% genny and 1 main reef to achieve this). The boat immediately hove-to, and I was able to fix it underway.
2) After reefing the genny on the roller furling in 20 knots and sailing pretty hard again, the roller ended up slipping allowing the reef to come out. With the drum now spinning independantly of the torque tube, I had to send the unit back to Harken for repair and replacement of a part or two. Fortunately, this happened the very last day of our vacation, so we had plenty of sailing. We'll see how this issue turns out, but I'm glad it happened there instead of on a trip with the family when we might really need it.
Overall, I am very pleased with the results, and glad to be sailing again! Here are some pics...
1) Repaired cracks and gouges, epoxy filled holes for mounting hardware, and painted hull and deck & binnacle with Interlux Perfection
2) Rebedded all deck hardware, replacing cleats and organizers
3) Built GPS housing and Engine control panel
4) Refinished hatches
5) Replaced chainplates (discussed in earlier thread)
6) Replaced Rudder with FOSS rudder - the improvement in handling is remarkable - better upwind perfomance, and and much better balanced helm. Also replaced quadrant with bronze as old aluminum one was siezed to shaft and significantly corroded. New chain as well.
7) New shaft, PSS shaft seal, and engine mounts
8) Replaced all thu-hulls - and relocated some. Enlarged scuppers to 2-inch, and moved them above the water line. There are four holes now below the water line (there were 8!) - raw water in, head discharge, sink discharge, and speedwheel.
9) Lightning grounding system.
10) Replaced all electrical wiring with marine grade tinned, and heat shrunk all terminals.
11) Replaced all engine hoses.
I sailed the boat hard the last weekend for sea trials in 20 knots (family was NOT onboard - took them out in 10 knots after initial trials). The biggest concern I had was the chainplate area, which I reglassed after cutting away a four foot by 2 inch section in order to remove old and corroded chainplates, and all of this held up beautifully during an intentional jibe (not a full force jibe, but wanted to test the rig with a sudden shock), and a minor knockdown.
The only things that went wrong were:
1) I lost steering b/c I had not tightened the u-bolts on the cable sufficiently (it took sailing closed hauled in 20knots after several trials with full 135% genny and 1 main reef to achieve this). The boat immediately hove-to, and I was able to fix it underway.
2) After reefing the genny on the roller furling in 20 knots and sailing pretty hard again, the roller ended up slipping allowing the reef to come out. With the drum now spinning independantly of the torque tube, I had to send the unit back to Harken for repair and replacement of a part or two. Fortunately, this happened the very last day of our vacation, so we had plenty of sailing. We'll see how this issue turns out, but I'm glad it happened there instead of on a trip with the family when we might really need it.
Overall, I am very pleased with the results, and glad to be sailing again! Here are some pics...